emkrueger830

Pitot Installation – Part 2
Did some rough trimming of the RH side fuselage side panel to verify routing path of pitot/aoa tubes. Disconnected RH rudder cable to ensure all bundles were behind it then reconnected cable to rudder pedal. Drilled 1/2″ holes through fuselage vertical channel and installed rubber grommets. Routed lines though grommets then up RH side of…

Pitot Installation – Part 1
Leveled fuselage then temporarily installed pitot mount into RH wing to calculate spacer size needed to level pitot tube. Made 2 0.125″ spacers (0.25″ total) out of 0.125″ aluminum sheet to place under back side of pitot tube mount. Installed mount into RH wing, checked levelness, then installed screws. Installed pitot mast into mount and…

ELT Installation
Located and drilled hole for ELT antenna on aft portion of turtle deck. Secured antenna to fuselage then routed and connected coax cable from antenna to ELT. Cut hole in RH #1 former for RCPI and drilled mounting holes. Installed vertical faceplate and A544 alkaline battery into RCPI (battery expires 06/19/2031) then mounted RCPI onto…

Cowl Fitment – Part 7
Continued to sand lower edge of upper cowling in preparation of lengthening the lower edge using hand and orbital sander with 60 grit. Finished rough sanding with 120 grit discs; should now be ready for fiberglass work. Cleaned upper edge of lower cowl with paint prep solution and applied packing tape to overlap area. Covered…

Cowl Fitment – Part 6
Began prepping upper cowl for fiberglass work by removing prop and spinner from engine then reinstalling lower cowl and cowl alignment spacer. Placed upper cowl into approximate position and secured to spacer. Traced 1.5″ line along upper cowl to mark limits of new fiberglass. Removed upper cowl and began to feather lower edge in preparation…

Card A – Fuel Flow Test
Configuration: Cowl removed; inspection covers for all fuel pumps and valves removed. Procedures: Results: Overall fuel flow rate from 19.25 gallons to 0.00 gallons was 22.95 GPH Gallons Time (Sec) Time (Total) Rate (GPH) 19.25 0.00 0.00 0 18 126.81 126.81 28.39 17 134.05 260.86 26.86 16 149.89 410.75 24.02 15 150.21 560.96 23.97 14…

Fuel Gauge Calibration
Calibrated fuel gauge by pumping fuel into tank from marked 6 gallon homebrewer’s bucket. Opted to calibrate fuel gauge in “ground stance” position (~8° nose up) and with ethanol free 91 octane mogas. Set points was recorded every 2 gallons per Dynon setup instructions. Due to probe length and aircraft attitude, probe reads full above…

Aileron Rigging
Created aileron neutral alignment tool with two rulers similar to the one used for flap rigging. Set neutral position for RH aileron and centered stick assembly using digital level. Adjusted aileron pushrod length via rod ends then secured RH aileron to control stick. Repeated process for LH aileron. Verified freedom of movement and range of…

First Engine Run Prep
Began preparing engine for first run by draining preservation oil from engine and replacing 3.7 quarts of Shell 15W-50 oil. Replaced oil filter with NAPA 1394 Gold oil filter. Removed and replaced all 12 NGK D9EA spark plugs and set gap at 0.023″. Torqued rocker cover bolts to spec. Installed Sonex exhaust pipes onto engine…

Stick Grip Wiring
Installed control stick ground wire and autopilot ground wire in GB24 ground block. Ran and routed PTT wires from mic jacks to stick grip harness and began populating fuselage side of connector. Attached aux fuse block power and ground wires to fuse block. Ran smoke system control ground to stick and left extra length on…

Control Frame Installation
Fabricated auto pilot push rod bracket from spare 2″ aluminum angle and bolted it to bottom LH side of control frame with AN3 hardware. Upon initial fit of the frame, discovered that aileron stops were contacting ends of spar tunnel bolts so trimmed approximately 3/8″ off each end of aileron stop. Stops still contact frame…

Fuel Leak Testing and Vent Installation
Added fuel to tank in order to test firewall forward side of fuel system. Upon opening fuel shutoff valve, discovered that hardline to system drain was leaking from both AN fittings. Upon removing the line, discovered that the flare fittings were not made properly. Remade hard line and installed new fittings. Leak checked firewall forward…











